Transport ministry is investigating the reason for the info loss following the worst-ever aviation catastrophe within the nation’s historical past.
The black packing containers holding flight information and cockpit voice recorders of Jeju Air’s Boeing 737-800 jet stopped recording about 4 minutes earlier than the aircraft catastrophe in South Korea in December, the nation’s transport ministry has stated.
Jeju Air’s Flight 7C2216 was flying from Thailand to Muan Worldwide Airport in South Korea on December 29, when it belly-landed, slammed right into a concrete barrier and exploded, killing 179 of the 181 passengers and crew.
It was the worst-ever aviation catastrophe on South Korean soil.
“The evaluation revealed that each the CVR and FDR information weren’t recorded in the course of the 4 minutes main as much as the plane’s collision with the localiser,” South Korea’s transport ministry stated on Saturday, referring to the 2 recording units.
The localiser is a barrier on the finish of the runway that helps with plane landings and was blamed for exacerbating the crash’s severity.
The voice recorder was initially analysed in South Korea, and, when information was discovered to be lacking, was despatched to a United States Nationwide Transportation Security Board laboratory, the ministry stated.
However it seems that the packing containers holding clues to the flight’s closing moments skilled information loss, leaving authorities looking for out what occurred.
“Plans are in place to analyze the reason for the info loss in the course of the ongoing accident investigation,” the ministry stated.
Sim Jai-dong, a former transport ministry accident investigator, informed Reuters information company that the invention of the lacking information was shocking and recommended all energy, together with backup, could have been lower within the aircraft, which is uncommon.
Investigators stated the packing containers had been essential to their probe however added they’d not hand over on looking for out why the crash occurred.
Investigators have pointed to a fowl strike, defective touchdown gear and the runway barrier as doable points.
The pilot had additionally warned of a fowl strike earlier than pulling out of a primary touchdown and initiating a go-around.
However as a substitute of constructing a full go-about, the Boeing 737-800 jet took a pointy flip and approached the airport’s single runway from the other finish, crash-landing with out touchdown gear deployed.
This week, lead investigator Lee Seung-yeol informed reporters that “feathers had been discovered” in one of many aircraft’s recovered engines, however cautioned a fowl strike doesn’t result in a direct engine failure.
Authorities have raided places of work at Muan airport the place the crash happened, a regional aviation workplace within the southwestern metropolis, and Jeju Air’s workplace within the capital, Seoul.
In addition they barred Jeju Air’s chief govt from leaving the nation.
Because the probe continues, transport minister Park Sang-woo provided his resignation earlier this week, saying he feels “a heavy sense of duty relating to this tragedy”.
